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30 December 2010

A new page!!. Reader's Cars.
This is your page to show off your cars. Simply email a picture and a brief description and I'll do the rest. No need to worry about picture size as I will resize to fit the page.

25 November 2010

It's a cold snowy day today so I decided to skive off going to work. I've spent some time in the warm adding a new page which gives some information on a very unique electric Vauxhall

21 November 2010

Last night saw about 50 members of the MG Car Club Tyne Tees Centre gather together for the annual dinner dance and prize presentation at the Gibside Hotel.

A night of good food and drink in great company with some gyrations on the dancefloor later.

Nobody was more surprised than Pam & I to find that I had won the Enthusiast Trophy and Pam won the Lady Enthusiast Trophy. We only did the events to enjoy ourselves but the trophys are a bonus.

If we look a little blurred in this picture, it's probably the amount of alcohol consumed.




6 November 2010

Things are quiet just now but there is still fun to be found. We set off in the BGT for the monthly natter and the car died. It just stopped. We got it back home and this morning I decided to investigate. Tuned the key and the silence was deafening. No tick tick tick as normal. I gave the pump a tap with a screwdriver handle and it sprang into life. I can feel a wallet lightening moment coming soon.

The 76 BGT is in the bodyshop, so apart from getting my spare Rostyles blasted and powder coated and cleaning up the brightwork there isn't much progress there.

24 October 2010

A cold but sunny morning saw
members of The Tees Valley MG Owners Club meet at Yarm Station for a run of some 34 miles, ending up at Shildon Rail Museum.  Thanks to Mal & Mary for organising this drive though some lovely countryside and along some superb roads.

We were delighted to see Mark & Mandy with their recently rebuilt 1947 MG TC making it's first trip of any distance longer than round the block. A lovely car and it performed faultlessly too.



A great day out in the company of good friends. That's what it's all about.

18 October 2010

What a weekend. We took a trip to deepest Cornwall to buy a 1976 MGB GT. Armed with a trailer (thanks, Steve, for the loan of it, and Bill for showing me where it was hidden) we set off  just before 10am on Friday and arrived at our hotel around 7pm.

Saturday morning saw us navigating narrow country lanes to find the car. It was as good as the seller said it was so we did the deal, loaded up and renavigated the country roads back to the A30.



The Audi pulled well and we were making good time until we came to a dead halt on the A30. After about an hour of stop start travel we passed the cause of the delay, a nasty accident, which according to the news had closed both carriageways for a while.

Travelling at 55 - 60mph made the 120 miles of the M5 a bit of a drag. The boredom was broken briefly by the sight of a chrome bumper roadster, top down, going past us like we were stood still, the driver giving us a big grin and thumbs up.

This turned out to be another 9 hour day and we were both cream crackered when we finally arrived at our overnight stop in Tamworth.

Refreshed after a good kip and a full English, we loaded up the car and found it wouldn't start. Eventually the RAC arrived and got us mobile again. We finally got the GT unloaded and into it's lock up around 3.30pm.



Now the work begins. My spare Rostyle wheels are in for blasting and powder coating to replace the tatty ones on the car. The body is in great condition but the paintwork isn't the best so It's going for paint when the painter can fit it in. In the meantime there is much to do.

20 September 2010

Stolen 1967 MGB NAL 57 E

Some despicable low life deprived an owner of his pride and joy. Taken from Anglesey in North Wales, this beautiful car is all original with only 18,100 miles on the clock.



If anybody knows the whereabouts of this car or has any information about its theft, please contact me or the police.

5 September 2010

The Old Speckled Hen Run is one of the three big runs organised by the Tyne Tees Centre of the MG Car Club.



We were roped in to do the signing on so we had an early start to the day. Signing on was great as we met everybody and put some names to faces. How long my memory banks will hold those names is another question.


The start was at the Windmill Hotel on the A19 and the run was about 100 miles, ending at Raby Castle, which is about 15 miles away as the crow flies.



The weather was kind to us and we had a great run. I don't think anybody had any problems on the run but one MGB had a slight issue of a split fuel pipe when setting off for home. This was soon fixed by using a short length of the radiator overflow pipe to replace the damaged bit.

We also used the day for a trial of a new camcorder, which turned out not too bad. I think some form of mount is needed as Pam said she had a hard time keeping it steady. I'm not sure if that was down to her or my driving.



After having our cream tea I took a couple of a short runs in the TA for people who wanted to see what it was like to travel in. It's a bit bouncy.



All in all it was a super day and a huge thanks go to Barrie and Sheila Hope for all their hard work in organising the run.

29 August 2010.

We had bright blue skies as we set off in the TA for Hamsterley Hoppings to join a group of friends from the Tyne Tees Centre of the MG Car Club.





Despite the blue skies it was cold with a bitter strong wind. Thankfully we had an almost dry drive up with only a few spots of rain unlike the unlucky souls who came from the North. They had torrential rain on their trip.

Apart from the MGs there were many other classic cars there. One noteworthy one was the Delage with it's wonderful straight eight engine. I can't remember if it was 5 or 5.5 litre.



The other was an electric conversion on a Vauxhall chassis, built in the 1930s. The current owner has promised to send me some information on this incredible car. When I get it I will do a write up on it.



Some heavy rain in the afternoon dampened eveything but our spirits and we thoroughly enjoyed the day.

This year the supported charity was Help for Heros. We hope they raised plenty for them.

28 August 2010

All is well now I have been refunded for the dodgy brake master cylinder. Hooray!!

22 August 2010

A bright sunny day saw a group of Tees Valley MG Owners set off from Yarm Station for a lovely run through Yorkshire countryside ending up at the delightful village of Hovingham. We had exclusive parking on the village green.





It was just the right weather for a picnic. Some of the posher ones had tables and pot cups.



After filling our faces we then did a walkabout treasure hunt in the village which was great fun even though we didn't win. A cuppa and slice of cake in the village tea rooms added to the pleasant day with good friends.

A big thank you to John & San for organising the whole day.

The BGT wasn't the ideal car for the weather but the TA is currently lacking in the tyre tread department and had to be left behind.

19 August 2010

I finally made contact with the master cylinder supplier and they have agreed to refund. The cylinder is on its way back to them. Time will tell.

15 August 2010

The new brake master cylinder turned out to be not so good after all. After using the brakes it wasn't fully releasing pressure and the car was getting slower and the brakes hotter. Letting it sit for a while would bring it back to normal, then the problem would return. I stripped the old cylinder and it was in good enough condition to fit new seals, so that's what I did. It went back in this weekend and all is now well again.

I don't like spending my hard earned on faulty goods so I emailed the supplier and still haven't had a reply some seven days later. I can understand that problems can happen but I believe the real test of a good company is how they put things right when they do.

Up to now, this company isn't doing very well. I'm not going to name them just yet. I'll do some more chasing first.

9 August 2010

Impressions of an automatic MGB GT.

Last week I got the chance to drive a pretty rare beast. Bill Marchant let me drive his very smart GT.





Ok, it looks like any other B until you get inside.



There you see the normal automatic 'gear' lever and the larger brake pedal.

Driving was a smooth experience. The auto box changes were almost unnoticeable, both up and down the box. Accelleration was slower than a manual,as expected, but nowhere near as snail like as I was expecting. Using the kickdown really made the car come alive.

The short drive I had was enough to show me that this is a very useable car with good performance and the engine should last forever as it's impossible to over rev it. Thanks, Bill for letting me have a go. 


25 July 2010

Today we took the TA to do the the 2010 Tees Valley Trail. This annual event is run by the Tees Valley MG Owners Club and this year was a run of 92 miles through some beautiful countryside with the added challenge of questions to answer along the way.



42 cars started the run and I believe all made it safely home to the finish. A wide range of ages from a 1934 PA right through to modern MGs.





The weather was kind with bright warm sunshine at the start and only cooling off towards the end of the afternoon. Thankfully there was no rain to speak of and everbody we spoke to thoroughly enjoyed the day.

Thank you to Geoff Brown and John Barton and their helpers for a superb day.

22 July 2010

The new master cylinder for the BGT arrived yesterday. I managed to get it fitted the same day but ran out of time to do the bleeding. With the help of Pam and her pedal pushing experience I got the brakes bled today and all is now well. I have to say that changing the master cylinder wasn't the easiest of jobs, partly due to the design but more to do with 39 year old fastenings refusing to respond, but that's life.

18 July 2010

Today was the great show and autojumble organised by The North East Club for Pre War Austins held in the beautiful grounds of Newby Hall. This is a massive event with just short of 1400 vehicles there according to the lists.

It was a great day, even though I didn't find all I wanted at the autojumble. The weather was reasonable and the threatening rain turned out to be a short, very light shower.





It was a great day and we met some old friends and made some new ones. After walking what seemed like miles round the field we gave our weary feet a rest and took a short steam train ride.



11 July 2010

After the good comes the bad. Out for a drive this afternoon in the BGT and on the way home I suddenly found a brake problem. The pedal went straight to the floor. Luckily on the second pump, it came back good & firm so I carefully limped home.

Investigation revealed a full master cylinder and no sign of any leaks, so it looks like digging into my wallet again for a new cylinder.

Luckily there isn't any great rush to get it done as the next runs will be in the TA.

9 July 2010

Last night at the MGCC Tyne Tees Centre natter I was discussing the fact that the overdrive on the BGT didn't work. The previous owner said it was a bit iffy. One suggestion was to switch it in and out a few times and see if it would come to life.

On the way home I tried just that and after a few tries it finally came in but with a delay of about 10 seconds from switching. A few more goes got the delay down to a second or so. As I was nearly home I left it at that.

Tonight Pam & I  went out for a drive and after a bit more use the overdrive comes in almost instantly. No Bachman, no Turner but I've got overdrive.

What a difference it makes. The car is much more relaxing to drive.


26 June 2010

Last night saw one of the MGCC Tyne Tees Centre's famed supper runs. I didn't count them but I think there were a dozen cars started from the motorway services near Durham, for the 35 mile run through glorious countyrside to the New Board Inn at Esh, where a large table was reserved.





The view from the inn across the valley was stunning and this picture from my phone doesn't really do it justice.



The New Board Inn is a great place to eat. Superb food at reasonable prices. Everybody ate well and the conversations flowed well to make a very enjoyable evening. Big thanks to Pete and Sue Sewell for their time and effort in organising this run.

20 June 2010

The 40th Beamish Reliability Trial, with a commemorative plaque for the event.



The modern event has been running longer than the original!

It was a cool overcast start to the day but it soon warmed up to the extent that I was driving in short sleeves in the TA. That's a rare thing on The Beamish.


All in all it was a great day with the opportunity to see some great vehicles and meet some super people.

The TA ran well with no signs of the mystery misfire. The only fly in the ointment was this.




Yep, my attempts at sealing the rocker cover failed. It didn't stop us from doing the whole run, we just contributed to oil company profits. Another job to do. If I can't stop the leak, I'll have to rename the car. How does Exxon Valdiz sound?

The lunch stop at Bainbridge was busy as normal.



The fine weather showed the beautiful countryside off to its best.





I spoke to one of the marshalls at the finish and all cars were accounted for and there were no cars unable to finish. That is a first I think.

19 June 2010

During the course of the week I got another working fuel pump fitted to the TA and it had a trial run on Thursday evening. We did a short treasure hunt with the Tees Valley MG Owners Club and the car ran well. Even the mystery misfire wasn't there, which was a great bonus. A bigger bonus was winning the event and taking home a nice bottle of red wine!

On the way back home as night was starting to fall, I had my lights on. About half a mile from home a Police car came up behind me. I was within the speed limit so didn't think anything of it. Suddenly the instant laxative, blue lights, appeared in the mirror. I stopped and the officer pointed out that I had no rear lights at all. Looking suitably glum I waited for the ticket, but he asked where I was going and how far it was. I told him and he said he was going that way and would stay behind me to cover my rear until I got off the main roads and into the estate. What a guy! Thank you.

Today was the first chance I had to investigate the lack of lights and it turned out to be two bulbs blown. Not only the tail light elements but the brake light elements as well. Two new bulbs sorted that. I wonder if the issues of a loose battery connection the previous weekend had anything to do with it. Hmmmmm.

Tomorrow is the 40th anniversary of the Beamish Reliability Trial, and I also spent some time today checking things over and adjusting brakes ready for some serious driving. All sorted I nipped off to top up with fuel and check the tyre pressures. On the way home smoke started to pour into the cockpit and a glance in the mirror revealed a trail of smoke behind me. Thick blue smoke. I pulled into a layby and opened the bonnet. The rocker cover gasket was leaking and oil was running onto the exhaust manifold.

As I was only a mile from home I pressed on. Not a hope of finding another gasket today so to make the Beamish tomorrow, I resorted to taking the cover off, cleaning it and applying liberal amounts of RTV. It seems to have stopped the leak but here's hoping it holds tomorrow. 

13 June 2010

The last couple of weeks have been pretty horrendous on the car front. The Audi decided to set up in competition with Hellmans in making mayonnaise. First and natural thought was head gasket, so off came the head. It was skimmed, pressure tested and replaced with new gaskets, the cooling system thoroughly flushed and it was up and running again. This took about a week and left me with a severe pain in the wallet. It wasn't running for long though as 10 miles later it was back in production again. Further investigation revealed that the oil cooler was leaking oil into it's water jacket. For those not familiar with Audis what they call an oil cooler is a box about 5" square that fits to the oil filter housing and has a water jacket round it. How the heck hot water is supposed to cool oil is anybody's guess but that's Audi for you.

Whilst this was going on, the TA had its MOT and failed. A few minor things, soon sorted and I got the retest done in time for the MGCC Tyne Tees Centre Prince Bishop's run from York to Durham, today.

On the way to York, the misfire that I thought was cured, reared its ugly head again and we were later than we wanted to be at the start.  We set off on the run well enough, living with the intermittent misfire until the car finally died. There was absolutely no electrical power at all. The battery isolation switch hadn't come adrift so it was dig down to the battery time and sure enough one lead was loose. I tightened it, or so I thought and we were on our way again.

A few miles further on we came to a halt again.  Straight to the battery this time and I made sure that the lead was tight. The car started and ran roughly for about 30 seconds then died. There was spark at the plug leads so the next step was fuel. I lifted the top of one float chamber to find it dry. Ther was no clicking from the solid state SU fuel pump so I took the cap off it to be greeted with the recognisable odour of burnt components.

That was the end of the journey for the TA and we called the RAC. Eventually we were recovered and taken home. It was a bit of a damp wait.





Once we got home and the TA safely back under lock and key we set off in the BGT to the finish at Durham for a chinwag and coffee. It was a wet finish to the day.





I must say that I've had better days, but it was still fun. The work begins now to get the TA sorted for the Beamish Reliability Trial next weekend.

23 May 2010

Strange happenings yesterday!. I decided it was time to cure the TA's misfire once and for all. A friend agreed to drive with me for a second opinion, so I set off for his place some 15 miles away. On the way there the misfire made itself known about 6 or 7 times.

On my arrival there was a very strong smell of petrol, which turned out to be coming from the front float chamber mounting point. This joint had always been damp when running, but never actually dripped fuel. When I tried to tighten it up the float chamber came off in my hand (honest Guv, it did). The thread in the body was stripped.

Luckily we found a box of carb bits and there was the right body in there. I fitted my existing dashpot and piston and float chamber, swapped the carb over, and it was running again. We went for a short run and I was amazed that the misfire didn't happen at all.

The run home was misfire free too.

Today we had a run with the Tees Valley MG Owners Club to Harlow Carr Gardens, near Harrogate.

We met at Yarm Station and had a pleasant drive down some lovely roads in blazing sunshine. We took a short coffee/ice cream stop in Masham, and arrived at Harlow Carr just after 12. No misfires at all up to now.

Harlow Carr is a beautiful place with plenty to see. We picniced and strolled around until, about 4, then set off for home.

Once again the misfire was noticeable by its absence. Dare I call it fixed? Why should changing the carb body make any difference? I can see nothing wrong with the old one apart from the stripped threads.

15 May 2010

We had a drive out to Leyburn today to see some superb cars at the lunch break of a VSCC rally. A great time only marred by the intermittent misfire on the TA becoming more frequent. Too many pictures to put them all here but these should give you the flavour of the day.





10 May 2010


What a great surprise in my inbox today! Because I'm always driving I don't have many pictures of my cars in action, but I got a great one here. Snapped by Trevor White near the CB Inn in Arkengarthdale. Thanks Trevor, I really do appreciate it.




Stolen MGA

Sadly some low life has deprived an enthusiast of his 1960 MGA Coupe. This is part of the email I received.

Sadly, my 1960 MGA Old English White Coupe, registration YXB 810, was stolen from Warners Hotel, Cricket St. Thomas on Saturday night 25th April 2010, whilst attending an MGOC weekend. I would be most grateful if you could e-mail your members to keep a look-out for this car should it appear at any shows or events or if anyone attempts to revise a car of similar description that has not been heard of for many years.

Chassis Number is GHD 82824 and Engine Number is 16GA 14153.


If you know anything or hear anything about this car which may be helpful, please get in touch and I'll pass the info on to the owner.

3 May 2010

I finally got the BGT propshaft off, new UJs in and shaft back on again. Whilst doing the job I noticed a scraping sound coming from the offside rear brake. The intermittent rain means I ain't going out to sort it today so the BGT is still on the axle stands.

The TA has a new tonneau. Custom made and quite a bit cheaper than ready made from Moss.



I'm often asked why I never have the hood up on the TA. Many reasons.

  • It's difficult for me to get in and out of the car with the hood up.
  • It's claustrophobic inside.
  • Visibility is severely restricted.
  • The hood was made in Nottingham from finest English lace
  • The hood spoils the lines of the car.
  • Hoods are for wimps.

1 May 2010

A weekend with no events so it's time to catch up on a couple of problems that have crept up on me.

The BGT has had a vibration for a short while now, which I've identified as universal joints in the propshaft. I got the front four bolts out but the rear four are proving reluctant (understatement of the year) to get out. The car is up on axle stands and I think it's time to attack the nuts with an angle grinder. One way or another the shaft is coming out this weekend.

The TA came back from last weekends Cobweb Run running a bit rough and lacking power. I spent about an hour going through the ignition system and timing with no benefit. I've found the problem this morning and I need to kick myself. I've preached for years that if you do something to a car and it gives trouble after, then the first place to look is whatever you last fiddled with.

In this case I'd decided before the Cobweb Run to try to drop the tickover a bit as it races when warm. I'd fiddled with the carb linkages to try to correct the problem, tested the car and all seemed well. This morning I had a look at the carbs and found that the linkage between the carb throttles was loose and the rear throttle was opening and the front one was still on tickover.

Thankfully an easy fix but I still feel an idiot for not looking there first. DOH!

An Evening with Miss Bridget

The Tyne Tees centre was host to Roy Locock and Miss Bridget, his super MG. Together they had travelled 39000 miles around the world and he was with us to give a talk about his travels.

About 50 of us enjoyed his talk about the adventures he had and the people he met and as well as having an enjoyable evening we raised a tidy sum for UNICEF.

Thanks to Roy for a great evening.

A date for your dairy. I'm keeping this at the top until after the event For the latest news, scroll down past it.

This should be a great night and definitely not to be missed. Come along and have a great time and support a worthy cause while enjoying yourself.

To book your place, contact
Peter@PeterEbdon.com or barrie.hope1@btinternet.com



25 April 2010

Today was the first of the MGCC Tyne Tees Centre's big runs. The Cobweb Run started and finished at Brockbushes Farm, near Corbridge where we had a dedicated parking area. The event was over subscribed as the MSA had limited us to 50 cars. One car failed to make the start because of overheating problems on the way there, so there were 49 who set off and completed the run of around 110 miles.

Cars ranged in age from my 1937 TA, the oldest, right up to modern MGs





The weather was kind to us, and although a little chilly on the hilltops, the rainclouds in the sky kept the wet to themselves and we had a great run. Lyn and Peter Ebden had found some stunning scenery and great driving roads, and thanks to them for all the hard work that went into making the day a thoroughly enjoyable one.

The TA had its, now customary, intermittent misfire on the way there, but performed faultlessly on the run. On the way home it began to run rough and lacked power, so there is some work ahead to find the fault.



As 25 April was 'Drive it Day', we saw other classic cars on the road, including about a dozen Morris Minors and some Lotus 7s or lookalikes (they were travelling a bit briskly to identify correctly.)

It was 61 miles each way to the start and with the 110 on the run it was another 200+ mile day.

17 April 2010

Twenty strong, they came, from the Southern flatlands to find the treasures of the North. Riding fine steeds, and led by Steve (The Intrepid) Trossell, they made their base by the bridge over the Greta. Seven steeds from the North found them there.





We ran with them for over 100 miles, through many counties, and realised that their leader had done well and found the treasures of the North. These treasures being the finest driving roads in the country through landscapes of the most stunning beauty. Treasures well found but thankfully not taken away.





All in all a very well planned run with good rest stops as well as superb roads. Some close parking at lunchtime.



After an excellent day in beautiful weather we arrived back at the start point and said farewell to a great group of people. We hope they have a trouble free run home tomorrow.

A big thank you to Steve for all the hard work that went into such a great day for us Northern lot, and what was hopefully a good weekend for the Flatlanders.

11 April 2010

Yesterday we went for a trip to the Lake District and decided to take the BGT as the TA has been a few times and we fancied something different. It was a beautiful day and a great run, even with a strange detour on the way. We were trying to find back roads across the hills and followed one, signposted to a village. After about 3 miles of poor single track road, we arrived in a farmyard and found the exit was closed with a gate carrying a sign saying 'Unsuitable for Motor Vehicles'. We turned round and retraced our steps. We weren't in any rush and as the views were superb, we just accepted it as part of the drive.

We eventually arrived at Windermere, where we stayed for abour 3 hours. Took a short cruise on the lake, had a great pub lunch and a wander about.

Leaving Windermere, we went looking for some passes to storm. Honister was the first and it was great. The BGT didn't have any problems at all with the climbs. I would have been surprised if it had. I was having too much fun to take many pictures, but here is one taken at the top of Honister.



After Honister, we went for Whinlatter, which is a much more gentle climb. Still an enjoyable one with great scenery. After Whinlatter we gave up on the passes because the traffic was surprisingly busy and [RANT] loads of idiot drivers who don't know the width of their vehicles[END RANT]. I lost count of the times I was tight up against a wall or had my wheels on the edge of a drop to make room for somebody who had a couple of feet between them & the edge of the road and still didn't think they could get past.

We cruised around for a while and finished up at Ullswater. I think Ullswater is the most majestic lake with the hills so close to the edge. After a relax with a cup of coffee we set off for home and arrive back about 12 hours after we left. Allowing for the stops we had we reckoned I'd been driving for 8 hours, and we'd travelled just short of 300 miles.

5 April 2010

I saw this super car in the local supermarket car park a short while ago.







I only had time for a brief chat with the owner and found out that it is a one off special built with Citroen 2CV mechanicals. As the body is steel, it's a bit of a sheep in wolf's clothing, and even though it has considerably more power than a standard 2CV, it hasn't really got too much in the way of performance. With a maximum speed of around 60mph, the owner reckoned that the 400 mile journey he was doing the next day would take about 10 hours. I hope the weather was kind and he made it OK.

We went for a drive out in the BGT yesterday, nowhere in particular planned, and we ended up stopping at the pumping station in Darlington. A fascinating place with the gas engine and the beam engine both working.

Both engines did the same job but the later gas engine made a lot more fuss about it. Compare the noise levels of the two.





Whilst we were there we bumped into an old friend of mine. I've known him for around 40 years, but lost contact some years ago. I was great to see him again and now we know where to find each other we'll be seing more of each other.

14 March 2010

The BGT has been running ok but not as well as I would have liked so I decided to have a look at the distributor. The initial plan was to fit an electronic module but there was significant wear in the dizzy so I started a search for a replacement. I found this guy http://www.simonbbc.com.

At £59.99 for a complete new dizzy it was worth a chance and I wasn't disappointed. It was a simple swap over, just pull the old one, put in the new and that was that. Unfortunately the timing light was broken so it's just set approximately for now, but even so the difference is noticeable. I realise that some of the difference will be down to a new dizzy compared to a worn one, but I'm still impressed and no more points to worry about.

This morning, the Flying Scotsman Rally made an appearance in the area. This is a very competitive event for pre 1941 cars who run from Brooklands to Edinburgh in 3 days covering a wide variety of roads. Tests are carried out at various points and today the cars were in Shildon.

What a mouthwatering selection of the best of, mainly British, cars all looking well used after the first two days. This morning was the start of the last leg to Edinburgh.

Feast your eyes on these.









It now becomes obvious that these cars are certainly not trailer queens.



It was certainly worth me getting up at daft o clock on a Sunday morning.

21 February 2010

A small group of half a dozen cars set off from Yarm Station heading for Bowes Museum in Barnard Castle.

This hardy group of members of the Tees valley MG Owners Club saw a fluttering of snow as they set off but it soon turned worse.







This was the state of play on the approach to Richmond so we stopped there and decided to go our seperate ways.

Pam & I decided to chance it and headed for Bowes. Despite the worsening road conditions we made it with only a couple of opposite lock moments at low speed.



After a good look round the Museum, a cuppa and slice of cake, we set off for home, expecting a longer than normal journey. The Gods must have been pleased with us as the roads were clear and we had a good run home.

20 February 2010

Today saw a group of MGCC Tyne Tees Centre members gather outside a typical modern unit on an average industrial estate. Inside, though, this was no ordinary unit, it was home to Heritage Classics.

Inside was a droolmaking selection of wonderful cars and superb workmanship. John and his team really work their magic to bring tired classic cars back to life.







Thank you to John and his team for your great hospitality and your patience in answering the multitude of questions fired at you.

7 february 2010

On Friday I received what I think is one of the most useful accessories for the MGB.

This neat device attaches to the headrest stalk and keeps your seatbelt where you can get to it instead of having to scrabble around behind the seat for it. Suitable for both the GT and roadster with the single post headrests, this really does work and has my wife's seal of approval and that isn't easy to get. It's made from moulded plastic and has the MG crest on the front and rear.

As all it does is guide the belt, it doesn't affect the safety or operation of the belt in any way. We gave it a good test today with a run from Stokesley to Helmesley, which anybody aware of the road will know is a twisty road with some steep climbs and descents. Even with some spirited driving  the belt stayed in place over our shoulders and we both felt comfortable with it.

We met some friends in Helmesley and showed them the holders. They were impressed too and wanted to know where we got them.

They came from a US enthusiast who makes some neat accessories for MGs and some other cars. Website is www.clarkandclarkinc.com

If the parts aren't on the website yet, drop them an email and Robert will be only too pleased to help.

I have no affilliation to this company. I'm just a very satisfied customer.





24 January 2010

Before  the snow arrived I had the misfortune to have an oil cooler feed leak and empty the sump. The leak was caused by the line from the back of the block sagging down and resting on the steering column joint. It must have been like that for some time and it finally wore through. Luckily I noticed the lack of oil pressure and switched off before any damage was done.

As the car lives outside and the snow came fixing it was going to have to wait.

The snow has finally gone and the BGT is back on the road. Oil leak fixed, fuel leak fixed, sailed through the MOT.

Here is a short clip of the climb up Carlton Bank.







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